Friday, January 29, 2010

67

After running the timing with it spot on the "ball" I found that I had to change it. Start-ups were harder and the low end had stalling issues. Power was good above 2000 RPM, but with the other issues I had to change it. So I tweaked the timing a little counter clockwise (advancing it). This improved the start ups and low end issues plus didn't take away on the power. So since everything seems to be going good with it right now I decided to try another speed run. I managed to run it almost to 70 while following some other cars, but the good thing is that it could have done more. The biggest thing is that there was no vibration from the driveshaft that I could tell, although the steering wheel had a little, but I think this is because I need an alignment.

Tomorrow I'll be tearing into the car to do some much needed maintenance tasks. Rear seat belts will be one of the first things on the list. I need to adjust the rear brakes and e-brake. The shift linkage will get some new pieces also. If time permits I'll adjust the hood and maybe replace the doors. Oh and a valve adjustment.

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